Thursday, June 13, 2013

SONY TRINITRON KV28LS60 - KV32LS60 - SERVICE MODE - SELF DIAGNOSTIC - LED BLINKING CODES


APPLICABLE TO
KV-28LS60B > RM-932 FR SCC-Q83C-A
KV-28LS60E > RM-932 ESP SCC-Q81E-A
KV-28LS60U > RM-932 UK SCC-Q84D-A
KV-32LS60B > RM-932 FR SCC-Q83B-A
KV-32LS60E > RM-932 ESP SCC-Q81D-A
KV-32LS60K > RM-932 OIRT SCC-Q82C-A
KV-32LS60U > RM-932 UK SCC-Q84C-A
SELF DIAGNOSIS
The identification of errors within the AE-6B chassis is triggered in one of two ways :-
1: Busy or
2: Device failure to respond to IIC
   In the event of one of these situations arising the software will first try to release the bus if busy (Failure to do so will report with a continuous flashing LED) and then communicate with each device in turn to establish if a device is faulty. If a device is found to be faulty the relevant
device number will be displayed through the LED (Series of flashes which must be counted) See table 1, non fatal errors are reported using this method. Each time the software detects an error it is stored within the NVM.
TABLE-1
STANDBY LED FLASH TIMING FOR 3 BLINKS
To clear the error count data press ‘80’ on the Remote commander.
ERROR MENU
  • Turn on the main power switch of the TV set.
  • Program Remote Commander for Operation in Service Mode.
  • Press ‘VIDEO’ ‘VIDEO’ > ‘MENU’ on the Remote Commander.
  • Using the Remote Commander, Scroll to the ‘Error Menu’ item using the down arrow key, then press the right arrow key.
  • The following table will be displayed indicating the error count.

TO ENTER SERVICE MODE
Service adjustments to this model can be performed using the supplied remote Commander RM-932.
  1. Press the VCR/TV/DVD button until the TV LED lights.
  2. Press and hold the yellow button for approx. 5 seconds until the TV LED flashes quickly.
  3. Press 99999. All three LED’s should light.  The remote commander is now set to Service Mode.
  • To return the remote commander to normal operation mode repeat steps 1. and 2. then press 00000. All three LED’s should light.
  • The remote commander is now set to normal mode.